(Sanitized) COMMENDATION
Document Type:
Collection:
Document Number (FOIA) /ESDN (CREST):
CIA-RDP63-00313A000600100112-1
Release Decision:
RIPPUB
Original Classification:
S
Document Page Count:
6
Document Creation Date:
December 20, 2016
Document Release Date:
October 26, 2006
Sequence Number:
112
Case Number:
Publication Date:
May 17, 1962
Content Type:
MF
File:
Attachment | Size |
---|---|
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Body:
Approved For Release 200SECRETIA-RDP63-00313A000600100112-1
Acting Chief, DPD
Chief Personnel Branch
Comma
Li)n
IDEA-0769-62
17 may 1962
25X1A
1. *V5 to Chief of Base, a le
Commendation in appreciation of the services rendered by
as Supply Officer of the Detachment.
2. Since the letter can not be incorporated in
military peroonnel file in be interest of Securi
far rour information.
r of
, it is attached
3. When the letter is returnect to S.eurity reneo, it vill be
tained permanently in the Sub c Agency Secfile.
Distribution:
1 - Acting Chief, DPD
1 - Chief, Personnel Branch, DPD
2 - SO/DPD
I - RI/DPD
25X1A
(rb
Approved For Release 2007/02/07:
Chief, Security BraeDPO
25X1A
25X1
25X1A
CIA-RDP63-0031/A000600100112-1
SECRET
25X1A
25X1
25X1A
25X1A
Dear
SECRET
Approved For Release 2007/02/07 : CIA-RDP63-00313A000600100112-1
IDEA-0770
Copy
of 3
17 May 1962
Encl9sed for your info are extracts from (1)
!Monthly UR Report and (2)1
Monthly Commander's Report. Seems as though most of our
problems fall in the inverter and autopilot area this
month. In the future I intend to forward extracts of
this type directly to you only for action you may deem
appropriate. This, I feel, will keep this UR reporting
from ricocheting off the walls at all levels. I know
we can get best results from this program with this type
of communication. Trust you will keep me informed of
any corrective action that can be taken to improve our
operation.
Sincerely,
25X1A
Attachments: 2
25X1A MS/DPT
Dist: Cy 1 H w/att
25X1A 2 - C/MS, w/att
3 - RI/DPD, Watt
ARET
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25X1A
25X1A
Approved For Release 2007/02/BRE1RDP63-09313A000600100112-1
MAINTENANCE MONTHLY UR REPORT
4-1. B-Spool, Part Number HI-732480-501. Bearings were
out of line. Casette shaft would enter bearings only under
binding condition. Spool was shipped to Hycon.
4-2. Inverter, Part Number SP-R419-2. Low voltage.
placed with serviceable part.
4-3. Mach Amplifier, Part Number SP-119611-03. Control
column pumps. Replaced with serviceable part.
4-4. Yaw Rate Gyro, Part Number SP-14500-1. Aircraft
heading squawk. Replaced with serviceable part.
4-5. Q Bay Safety Valve, Part Number SP6.103102-438. Cabin
pressure fluctuates. Replaced with serviceable part.
4-6. Inverter, Part Number SP-R419-2.
placed with serviceable part.
4-7. Inverter, Part Number SP-R419-2.
placed with serviceable part.
Low voltage. Re-
Low voltage. Re-
4-8. Attitude Gyro, Stock Number 6610-663-8800. Excessive
precession. Replaced with serviceable part.
4-9. J-75 Engine, Part Number .1-75-P13. Loss of engine oil.
Replaced Q.E.C.
4-10. Speed Brake Cylinder, Part Number SP-H5. External
oil leak. Replaced with serviceable part.
4-11. Inverter, Part Number SP641419-2. Low voltage.
Re-
placed with serviceable part.
4-12. Attitude Gyro, Stock Number 6610-663-8800. Excessive
precession. Replaced with serviceable part.
4-13. Hydraulic Driven Fuel Pump, Part Number SP-115364.
Cause unknown. Replaced with serviceable part.
Approved For Release 200., tiCIA-RDP63-00313A000600100112-1
El
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MONTHLY COMMANDER'S REPORT
I. In Headquartess Message 0400, dated 27 April, you re-
quested additional details on autopilot discrepancies
mentioned in last month's report. Following is a detailed
resume for the Month of March prepared by our Autopilot
Tech Rep:
25X1A
a. Summary of Flights on Article 358:
Flight 1 Write up: Overshoot out of righ turns
Correction: Recalibrated aileron axis
Flight 2 Write up: Overshoot out of both turns
Correction: Replaced multi channel in
main amplifier (Trouble did
not recur)
Flight 3 Write up: Mach Sensor out
Correction: Found broken wire at Mach
Sensor pot, resoldered
(Trouble did not re-occur)
Flight 4 Write up: Intermittent yoke pumps
Correction: Recalibrated pitch axis
(Trouble did not re-occur)
Flight 5 Write up: All axis sloppy
Correction: Replaced inverter (Trouble
did not re-occur)
Flight 6 No Write up.
Flight 7 Write up: Intermittent rudder drift
Correction: At this time, the Article
went in for 100 hour inspection. At
this time, many components were replaced
due to time change requirements.
Flight 8 No Write ups on Test Flight. Since this
flight, we have had five flights on this article
with no autopilot write ups. Upon receipt of
this Article, it did require much "cleaning up"
of minor problems in order to staisfy
our local mission.
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b. Summary of Flights on Article 352:
Flight I No Write ups
Flight 2 No Write ups
Flight 3 No Write ups
Flight 4 Write up: Slow to recover from turns
Correction: Recalibrated aileron axis
(Trouble did not re-occur)
Flight 5 Write up: Run-away down trip
Correction: Recalibrated trim servo
amplifier
Flight 6 No Write ups
Flight 7 No Write ups
Flight 8 Write up: Article nosed down,
appearing to be run-away
axis
Flight
Correction: At this time I suspected a
OCG. problem because both
nose down conditions had
occurred with approx 500
gallons of fuel remaining.
We increased ballast to 50
pounds.
9 No Write ups. Pilot did use full nose
up trim, thus we reduced
ballast to 20 lbs
Flight 10 Write up: Article nosed down with
approximately 400 gallons
fuel remaining.
Correction: Found pitch clutch torque
low--increased to 55 lbs
Flight 11 No Write up: Pilot did use full nose
down trim and did notice an
excessive load on the yoke
at approximately 400 gallons
remAining fuel. I suggested
using 30 lb ballast.
ApprovedForiWeWsee2097611/57ke-tRIDIDI6131313A000600100112-1
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Approved For Release 2007/01ARRR-RDP63-00313A000600100112-1
c. All trim problems with Article 352 were occuring
at approximately 500 to 400 gallons remaining fuel lad.
It is my opinion that due to improper C.G., there was not
enough trim available. This caused excessive loads on the
system and the clutch was slipping at this time. I feel
that Wan the Article is weighed after IRAN and a new basic
weight is established the problem will be eliminated.
d. Replacement Parts: During the 100 hour inspection
I returned two items drawn from stock:
(1) Mach Sensor Control - found a weather
checked hose
(2) Pitch Trip Control - could not calibrate
the unit to within the proper range.
Theme are isolated cases, as most parts received hare been
aceepatable. The problem with the items has been noted on
the repairable tags attached to the repairable items.
SECRET
Approved For Release 2007/02/07 : CIA-RDP63-00313A000600100112-1