(UNTITLED)

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP66B00664R000600060078-4
Release Decision: 
RIPPUB
Original Classification: 
S
Document Page Count: 
2
Document Creation Date: 
December 14, 2016
Document Release Date: 
October 9, 2002
Sequence Number: 
78
Case Number: 
Publication Date: 
July 2, 1964
Content Type: 
CABLE
File: 
AttachmentSize
PDF icon CIA-RDP66B00664R000600060078-4.pdf134.87 KB
Body: 
naviqjs ATiO roved For Release 200. 0 6 066 ''AT 1005Z 02 JUL 64 25X1A TO DIIECTOR I CTK)N 00,5 INFO TOR 1215Z 02 JUL 64 25X1A TO 25X1A 25X1A 4-Lo I CL 2 a __ w 53 14 16 PRIORITY IN 86326 25X1A 1. T 4Y- MALFUNCOT ION CAUSING AUO T ON MSN 134 C OCCURED TWO H(0 U.RS PLUS 21 MIN AFT TAKE OFF. THE INDICATIONS TO THE PILOT WERE AS FO LLO W 5: A. THE BATTERY DISCHARGE LIGHT ILLUMINATED FOR 5 SECONOS0 THE LOADMETE'R SHO JED A STEADY .5 APPEARED ON THE GYRO HORIZON eo THE OFF FLAG D A RATHER BRISK LEFT WING AND NOSE DOWN MOMENT WAS INTRODUCED BY THE AUTO PILOT JUST PRIOR TO AN AUTOMATIC DISNNGGAGEMENT. E. THE PILOT LEVELED THE AIRCRAFT AND SELECTED NO0 2 INVERTER. F. THE LOADMETER RETURNED TO NORMAL of r ,25 0. AUTO PILOT ENGAGE KNOB WOULD TURN TO ON POSITION BUT NO AUTO PILOT FUNCTIONS WERE AVAILABLE. ALL OT HE' INVERTER POWERED INSTRUMENTS EXCEPT AUTO PILOT OPERATED NORMAL ON NO. 2 INVE TERM H. MSN WAS ABORTED DUE TO AUTO PILOT. 2. AFTER THE AIRCRAFT LANDED MAINTENANCE INSPECTION REVEALED THE FOLLOWING: E w i ? . R, z:l ffecm a~tertzuPic .r S6~!IQ AfiL,~ Approved For Releas ae~20a~02s/1t AO ~1pt- 6ARRDP66BO 66 ROO p~ so - py ?9 C'iiDf"4['a!E#"'~'~~`l Y ?T5 Htl! 261,c`F.s 9 HF' SS$UII G OFFCCE CS PP~~H ! D. Eopy Ht Approved For Rel se 2002/10/29 : CIA-RDP66B00664R 600060078-4 ( IN 861-326) S E C R E T PAGE TWO A. THE AUTO PILOT YAW SYNCHRONIZER, P/N 83130-R492?2, WHICH IS A SEALED UNIT WAS FOUND SHORTED OUT. WHEN THE UNIT WAS REMOVED EITHER BROKEN OR LOOSE PARTS COULD BE DETECTED INSIDE WHEN THE SYNCHRONIZER WAS MOVED FROM SIDE TO SIDE. THIS SYNCHRONIZER IS A COMPONENT OF THE MAIN AMPLIFIER WHICH WAS INSTALLED 2.6 HRS PRIOR TO THIS FLIGHT. OPERATION WAS SATISFACTORY ON PRIOR SHAKEDOWN FLIGHT AND ON MSN 134C UNTIL LOOSE PARTS CAUSED. A SHORT. WE HAVE NO WAY KNOWING HOW THE PARTS INSIDE WERE BROKEN OR BECAME LOOSE BUT SUSPECT ROUGH HANDLING. THIS UNIT HAS BEEN CARRIED AS A SPARE SINCE MARCH 64 AND HAS BEEN MOVED SEVERAL TIMES INCLUDING A VERY ROUGH TRUCK RIDE FROM B. WE BELIEVE THAT THE EXCESSIVE ELECTRICAL LOAD AND FAILURE OF THE NO. 1 INVERTER WAS CAUSED BY THE SHORT IN THE YAW SYNCHRONIZER. 3. THE MAIM AUTO PILOT AMPLIFIER AND THE NO. 1 INVERTER HAVE BEEN REPLACED, AND BOTH UNITS INDICATE NORMAL OPERATION ON GROUND CHECKS. END OF MESSAGE Approved For Release 2002/10/29 : CIA-RDP66B00664R000600060078-4 S F C R E T