PROGRESS REPORT ON FOUR-INCH ROCKET FOR NOVEMBER 1954

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP78-03624A000900010055-1
Release Decision: 
RIPPUB
Original Classification: 
C
Document Page Count: 
3
Document Creation Date: 
December 23, 2016
Document Release Date: 
August 7, 2013
Sequence Number: 
55
Case Number: 
Publication Date: 
January 3, 1955
Content Type: 
REPORT
File: 
AttachmentSize
PDF icon CIA-RDP78-03624A000900010055-1.pdf160.58 KB
Body: 
Declassified in Part - Sanitized Copy Approved for Release 2013/08/07: CIA-RDP78-03624A000900010055-1 CONFIDENTIA 3 January 1955 ORIGINAL CL 7 5 DECL ErgrrNIN ON 7---0 / EXT BYND 6 YRS ISY 4241/6- REASON 3 cv..(3J (PROGRESS REPORT 50X1 DOCNZ- ORM COMP ORM CLAS JUST R V DATE 29 ","9AJ, By oz.F373 DPI 51 TYPE 03 PAGES REV CLASS KEN REV 2OLLLA__ ADM: MR 104 AMOISM11.1?11.111.1011?11.... ON FOUR-INCH ROCKET FOR NOVEMBER 1954 CONFIDE IT'AL im Declassified in Part - Sanitized Copy Approved for Release 2013/08/07: CIA-RDP78-03624A000900010055-1 Declassified in Part - Sanitized Copy Approved for Release 2013/08/07: CIA-RDP78-03624A000900010055-1 The month of November was spent in testing various types of non-metallic materials which might be employed in the fabrication of the head plate for the multiple motor rocket. Greatest emphasis was placed on laying up a combination of glass cloth and polyester resin since it was felt that glass reinforced resins would furnish more strength than any other known plastic or combination plastic material. A number of different lay-up techniques were used in an effort to obtain greatest strength in all directions since the chamber pressure forces are applied in all directions. A material consisting of flat disks of glass cloth, lami- nated together with polyester resin was machined as a one piece head plate to receive the individual motors. Upon static test firing, delamination of the layers occurred with resultant failure of the test motor. Another one piece head plate was laid up by rolling poly- ester soaked glass cloth of two inches width into a con- volute cylinder. After machining, this motor head was tested using six motor tubes. Again delamination occurred but in a direction parallel to the axis of the motor. Other materials tested included celeron, a combination of epoxy resin and aluminum powder, rag filled phenolic, hard maple wood, and paper laminated phenolic. All these ma- terials failed to withstand the pressures encountered and ruptured. Although these materials had been previously tested as a part of the original motor design, it was felt that a redesigned one piece head plate, with the cap and tail plate eliminated, would reduce strength requirements thereby permitting the use of at least one of the materials mentioned above. The tests made on these materials indicate that no non- metallic material alone possesses sufficient strength in all directions to permit use as a head plate. Consequent- ly the most logical approach to be taken from this point forward appears to involve the employment of a network of plastic tubes, such as have been used as motor tubes, con- nected by a central chamber. This would permit the utiliza- tion of the great hoop strength of these materials in with- standing the pressure encountered. This network of inter- connecting tubes could then be imbedded in a thermo setting plastic to obtain rigidity. Holes designed to receive in- dividual motor tubes could then be machined into the plas- tic and into the reinforced tube network. -2- r 11 Declassified in Part - Sanitized Copy Approved for Release 2013/08/07: CIA-RDP78-03624A000900010055-1 Declassified in Part - Sanitized Copy Approved for Release 2013/08/07 : CIA-RDP78-03624A000900010055-1 ? ; I This system would eliminate considerable machining and would thereby be more satisfactory from a production standpoint. Construction of this type of head plate is now in progress. A series of tests were conducted for the purpose of deter- mining whether or not plastic nozzles with metal inserts could be glued into the plastic motor tube with sufficient adhesion to prevent breakage when exposed to the pressure of a burning grain. These tests were very satisfactory and indicated that this system of nozzle insertion can be used. Further tests, using retaining rings to suspend the indi- vidual motor tubes into the head plate, were conducted. These tests were equally satisfactory. Several grains were burned in the plastic motor tube using the retain- ing ring suspension system with no apparent damage to tube, ring or head plate. In addition to this type of motor tube suspension, another method has been tested satisfac- torily. This method involves only the gluing of the mo- tor tube into the head plate with an epoxy resin. Several such grains were burned satisfactorily in tubes suspended in this manner. Plans for Future Work Work on this program will continue as outlined above and in previous progress reports. It is believed that as soon as a suitable head plate can be designed and built, the task of fabricating and flying a test rocket can be accom- plished. Financial Statement Total Amount of Contract Expenditures During November 1954 Total Expenditures to 30 November 1954 Total Unexpended Balance Declassified in Part - Sanitized Copy Approved for Release 2013/08/07: CIA-RDP78-03624A000900010055-1 50X1