HOCHSEESCHIFFBAU WARNOW-WERFT, WARNEMUNDE

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP82-00457R010500400009-6
Release Decision: 
RIPPUB
Original Classification: 
S
Document Page Count: 
2
Document Creation Date: 
December 22, 2016
Document Release Date: 
May 17, 2011
Sequence Number: 
9
Case Number: 
Publication Date: 
March 12, 1952
Content Type: 
REPORT
File: 
AttachmentSize
PDF icon CIA-RDP82-00457R010500400009-6.pdf209.42 KB
Body: 
Sanitized Copy Approved for Release 2011/05/17: CIA-RDP82-00457RO10500400009-6 CENTRAL I .rj ?_k..ICENC AGENCY REPORT t 3RIMATION, REPORT CD NO, Ge nnr. iay (k axssi.m' Zone) Hochseeschiffbau ?t arncwi-r''erf A D.DA ?F. DIST R 12 Mar 52 OF E CLS.. . 'W, 15 DOCU3IEHT CONTAIH3 1HFOR[.ATIOII AFFECYIHO THE RATIOYR:f. DEFENSE OF THE URITEO STATES. MTRtn 111: WEANING OF T1TLE 10, SECTIONS 709 ",{ ATlOff OF ITS CORTERTS !O OR RECEIPT ES A41 UNAUTHORIZED PERSON IS PROHUSITED BY LAR +RE RE1 RODUCTIOA OF THIS FORM 15 PROHISITED. V ; 1 l ,ry So.;a RUS J HIS IS UNEVALUATED INFORMATION 50X1-HUM ab In spite of siren,.ous efforts on the part of the Dockyard Directorate to get this vessel finished on time, it is row not expected to be completed. This delay i6 largely caused by the un;Dxpec e : an. flare of 3_ ts new y installed engines to function as anticipated bo Th:. two main diesel engines were uncoupled from the mainshaft and,given a trial run, which showed -the following - ieaknesses -- two cylinders on tht' port engine did not work at all; the starboard motor developed a major oil leak, and there was too much play on the engine bed rega3i.e ng a :'resh setting (neue Millimeter Unterlager), The ten workmen from the MAN factory at Augsberg are still in the dockyard and are supervising tho repairs to the engines which have been dismantled again and taken our; of the ship. Al'.;hough the former German degaussing p rdle switchboard has been over?hGul d with new .Luses, copper coils? isolators and distribr t,or?s and fil;ted and replaced in the ship., fo preparations have been made for the filling of a degaussing, fix cle It was observed that,, unlike the switchboard fitted into the ASia", last year, the switchboard now in the RU:S has leads for more lines of cahl as each switch box has '16 'irLre leads fitted to it