CABLE FROM (Sanitized)

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP89B00980R000300060028-6
Release Decision: 
RIPPUB
Original Classification: 
S
Document Page Count: 
3
Document Creation Date: 
December 15, 2016
Document Release Date: 
August 22, 2003
Sequence Number: 
28
Case Number: 
Publication Date: 
December 22, 1964
Content Type: 
CABLE
File: 
AttachmentSize
PDF icon CIA-RDP89B00980R000300060028-6.pdf136.92 KB
Body: 
Approved For Release 2004/05/13 : CIA-RDP89B00980R000300060028-6 DP E 1545Z 22 DEC 64 S E C R E T 25X1A DIRECTOR 25'X1;A 25X1.A FROM : ACTION, INFO 25X1A KEDLOCK 1.~FLIG HT NO 48, ARTICLE 1001, FLOWN MONDAY 21 DEC 1964 25X1A ,,. 3. DURATION: 0:55 HRS, TOTAL TIME 57:,45 HRS. 4. MAX SPEED REACHED: 3.15 M -MAX ALT 73,000 FT 5. TIME FROM 0.9 M TO 1.2 M APPROX 4 MIN 6. TIME FROM 1.2 M TO 2.0 M: APPROX 5 MIN 7. TIME ABOVE 2.0 M: 0:20 HRS THIS FLIGHT. TOTAL 6:11 HRS 8. TIME ABOVE 2.6 M: 0:15 MRS THIS FLIGHT. TOTAL 1-012 MRS 9. TIME ABOVE 2.8 N: 0:10 HRS THIS FLIGHT. TOTAL 0:40 MRS 10. TIME ABOVE 3.0 M: 0:05 MRS THIS FLIGHT. TOTAL 0:18 MRS 11. T.O. WEIGHT 115,600 LBS, C.G. 22.3 PERCENT 12. CONFIGURATION: SAME AS FOR FLT 47 EXCEPT RH CIT SYSTEM COMPONENTS CHANGED AND BOTH SYSTEMS RECALIBRATED TO COR- RECT PROBLEMS OF FLT 4x1. USAF review(s) completed. ..WNGNACINC Approved For R lease'2(f04/r0&1 f-: 6IA-RDP89 0098 NATIC 028-6 REPRODUCTION BY OTHER THAN THE ISSUING OFFICE IS PROHIBITED. COPY NO. Approved For Release 2004/05/13 : CIA-RbP89BOO98OR000300060028=6 25X1A 13. OBJECTIVES: PERFORMANCE ACCELERATION TO MAX MACH NO. YAW AND PITCH STABILITY EVAUATION UP TO 2.6 M. INS CHECK FOLLOWING FAST ALIGN SET-UP. 14. TAKEOFF AND CLIMB-OUT WERE UNEVENTFUL. TAKEOFF WAS MADE TO THE WEST, FOLLOWED BY TURN AROUND AND CLIMBING ACCELERATION TO THE EAST AS ON PREVIOUS YLIGHT. 15. TRANS-SONIC ACCELERATION APPEARED QUITE GOOD TO THE PILOT, AS DID THE REST nr THE ACCELERATION. S E C R E T (IN 64103) PAGE 2 16. CLIMB =CHEDULE FOLLOWED WAS SAME AS THE PREVIOUS FLIGHT. 17. INLE" OPERATION SMOOTH THROUGHOUT ENTIRE ACCELERATION. SOME MINOR UNSTI.TS AT 1.9 M - 1.8 M ON DECEL. 18. 3`-40 DEGREE BANK TURN STARTED AT 2.2 M, APPROX. SAME LOCATION AS ON PREVIOUS FLIGHT. 3.1 M REACHED BY ROLE-OUT. 19. SMALL YAW OSCILLATION, DAMPED, OCCURRED SEVERAL TIMES BETWEEN 2.98 M PAD 3.02 M, SIMILIAR TO LAST F1..IGHT. NOT CONSIDERED A PROBLEM. 20. ACCELERATION TERMINATED. AT 3.15 MACH WHEN LIMIT CIT REACHED 2$,5r10 LBS FUEL REMAINING AT THIS POINT. 21. CIT?S EX'{IBITED TEN DEGREE C SPREAD AT LOW SPEEDS, INCREASING :O 35 DEGREE SEPARATION AT PEAK MACH. THIS SAME AS ON PRE- VIOUS FLIGHT, SINCE EXTENSIVE CORRECTIVE WORK HAD BEEN DONE ON THE GROUND SPICE THE LAST FLIGHT TO ASSURE SYSTEM ACCURACY, IT 1S EVIDENT THAT SOME CONDITION ASSOCIATED WITH FLIGHT OPERATION IS FEEDING ERRJR INTO SYSTEMS. WHATEVER THE CONDITION, IT NOT ONLY CAUSED THE TWO SYSTEMS TO READ DIFFERENTLY, BUT BOTH TO READ HIGH. TOP PRIORITY EFFORT IS BEING APPLIED TO CORRECT THE PROBLEP.. Approved For Release 2004/05/13 : CIA-RDP89B0098OR000300060028-6 Approved For Release 2004/05/1'3': CIA-RDP89B00980R000300060028-6 25X1A S E C R E T I N 64108) PAGE 3 22. YAW AND PITCH STABILITY CHECKS OBTAINED IN THE DECEL FROM 2.6 M DOWN TO 1.4 M. 23. AUTOPILOT ALTITUDE HOLD MODE CHECKED AT 400.KEAS, 58,800 FT. EXHIBITED FAIRLY CONSTANT PITCH OSCILLATION WITH 2?3 SECOND PERIOD. 24. INS HAD BEEN ALIGNED AN HOUR OR TWO BEFORE FLIGHT AND ZURNED OFF EXCEPT FOR STANDBY HEAT. AIRCREW CONDUCTED FAST ALIGN AFTER ENGINE START. RESULTS QUITE GOOD: 8-9 N.MI. TERMINAL ERROR AFTER 80 MINUTES IN NAV MODE. 25. DRAG CHUTE OPERATION SATISFACTORY ON LANDING. CORRECTIVE ACTION NOTED IN TWX ON LAST FLIGHT APPEARED TO BE EFFECTIVE. 26. PHOTO PANEL TEST RECORDS NOT AVAILABLE AFTER APPROX. 0.9 M IN THE ACCEL. FILM TAKE-UP SPRING FAILED, JAMMING CAMERA. 27, PLANNING FURTHER INVESTIGATION INTO CIT SYSTEM PROBLEM BE- FORE NEXT FLITE. ALSO MUST CHANGE SEALS IN RH ENGINE TEB TANK FILL VALVE. CONSIDERING CORRECTING BOTHERSOME LEAKS IN NOS 1 AND 3 TANKS. WILL RESUME FLYING TUESDAY OR WEDNESDAY OF NEXT WEEK. END OF MESSAGE Approved For Release 2004/05/13 : CIA-RDP89B0098OR000300060028-6