CABLE FROM (Sanitized)

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP89B00980R000300060058-3
Release Decision: 
RIPPUB
Original Classification: 
S
Document Page Count: 
2
Document Creation Date: 
December 15, 2016
Document Release Date: 
August 22, 2003
Sequence Number: 
58
Case Number: 
Publication Date: 
December 16, 1964
Content Type: 
CABLE
File: 
AttachmentSize
PDF icon CIA-RDP89B00980R000300060058-3.pdf118.17 KB
Body: 
Approved For Release 2004105/13 : CIA-RDP89B00980R000300060058-3 185 0Z 16 DEC 64 tt;- 25X1A _. E C R E 1 7 ! LD I/1 1. FSW NBR 625 DISTRIBUTION, tH{:tS MESSAGE- LIMITED TO THOSE WITH ABSOLUTE NEED TO KNOWS 25X1A 2. FROM AREA SERVICE. 3. NO FL IGHZS--kCCOMPL ISHED ON 14DECEMBER . /ARTICLE NO 124 MADE GO 278. ON `15 DECEMBER. MAX ALT 43MMm1MMAA CC MACH 1.3 DURATION 1:10 PURPOSE, DRIVER TRAINING, NO ENGINE PROBLEMS. 5. ARTICLE 121 PRESENTLY HAVING R irNGINE (219) REPLACED BY 206. ENGINE .219 BEING REMOVED FOR INVEST IGATION OF STALL CONDITION ENCOUNTERED DURING GO NER 156 PER FSW NBR. ,624. 6, ARTICLE 122 MADE GO 83 ON :15 DECEMBER, MAX ALT 7405 MAX MACH 25X1A 2.84 TOGW 109.6K DRIVER DURATION 1:02 PURPOSE? PERFORMANCE AND ENGINE RE-LITE. NO TRIM PRIOR TAKEOFF AND NONE USED DURING FLIGHT. EGT ? S FOLLOWED THE OPERATING BAND-PRETTY WELL. THE RH ENGINE 256 WAS SHUTDOWN AT 2.0 MN THEN IMMEDIATELY RE.-LIT.: SOME INLET ROUGHNESS ENCOUNTERED BUT ENGINE RE-Li*Tg ABILITY WAS NOT AFFECTED. USAF review(s) completed. Approved F CROIVDIID FROM RUrO- NKtfO C^'NN6AADIMJ RMD OECUUStfCAY1ON Y?-Y. 1tdUGi3y !~ i-i ?" ? N i HE E; 4SS ii G OFFICE iS Pik?i iiBITED. copy mo. '!7 Approved For Release 2004/05/13 : CIA-RDP89B0098OR000300060058-3 25X1A 25X1A 7. ARTICLE 129 MADE GO 79 ON 15 DECEMBER. MAX ALT 78M MAX MACH 3.14 TOGW 121.8K DURATION 1:16 PURPOSE, PERFORMANCE. NO TRIMMING PRIOR TO TAKEOFF,, SOME ON EACH SIDE DURING FLIGHT. DURING TURN AT OUTBOUND END bF COURSE HAD SOME LEFT HAND NOZZLE FLUCTUATION. AFTER THE TURN LEFT ENGINE STALLED AND EGT NOTED AT 94 0 DEGREES C. REDUCED POWER TO MILITARY AND BELOW TO BRING EGT DOWN AND CLEAR THE STALL. RE-ADVANCED POWER TO A/B AND THEN NOTED 37,0910 PPH FUEL FLOW ON LEFT ENGINE-AND NOZZLE IN FULL OPEN POSITION. REDUCED POWER TO IDLE AND NOTED LEFT FUEL FLOW AT 10,000 PPH SO SHUTDOWN LEFT ENGINE AND RETURNED HOME ON RIGHT ENGINE. PRELIMINARY INVESTIGATION FOLLOWING LANDING REVEALED BROKEN LINE IN EXHAUST NOZZLE MANIFOLD OF THE "CLOSED" CIRCUIT. FURTHER DETAILS PENDING ENGINE REMOVAL AND SHOP INSTPECTION, 8. ARTICLE 131 MADE GO 30 ON 15 DECEMBER. MAX ALT 47M MAX MACH 25X1A 1.45 TOGW 105K DURATION 58 MINUTES PURPOSE, RADIO PACKAGES. HAD SOME FLUCTUATION OF LEFT HAND EXHAUST NOZZLE PRIOR TO TAKEOFF WHICH CLEARED AND NOZZLE THEN REPORTED AS OK FOR ENTIRE FLIGHT. NO OTHER PROBLEMS. Approved For Release 2004/05/13 : CIA-RDP89B0098OR000300060058-3