CABLE FROM (Sanitized)
Document Type:
Collection:
Document Number (FOIA) /ESDN (CREST):
CIA-RDP89B00980R000300060103-2
Release Decision:
RIPPUB
Original Classification:
S
Document Page Count:
2
Document Creation Date:
December 15, 2016
Document Release Date:
August 22, 2003
Sequence Number:
103
Case Number:
Publication Date:
December 3, 1964
Content Type:
CABLE
File:
Attachment | Size |
---|---|
![]() | 109.96 KB |
Body:
25.X1A
25X1A
Ap.pravid For Rele
0A; 2215 Z 03 DEC 64
FLIGHT NO. 31, ARTICLE 1@.2 FLOW.. P' DEC 1964.
3. DURATION: 1:20 HRS9 TOTAL TIPPE: 40':05 MRS.
4. MAX SPEED REACHED: 0.95 AR. 'MAX. ALTITUDE: 359400 FT.
5. TIME ABOVE 2.0 i'to 0:00 MRS THIS FLT. TOTAL: 2:19 HRS.
70
KEDLOCK
1.
2.
T. 0. WEIGHT: 115, 727 LBS.. C. G. 18.7 PERCENT.
0BJECTIVESo EXTERNAL WISSILC CAPTIVE FLIGHTS G?11.
8. ENGINE STARTS GENERATOR OPERAT IO.N, INNS ALIGNMENT, LIQUID
COOLING PACKAGE OPERATION, AND FIRE CONTROL SYSTEM TURN ON WERE .
SATISFACTORY.
9'. THREE PASSES WERE COHPLETLD USING. THE FOR 25X1
VECTORING. THE 6-57, AUGMENTED WITH DOPPLER AND NOISE AGUPIENTATION,
WAS AT 0.65 MAT 109000 FEET. THE YFO12A WAS AT 0.9 M AT 35,000
FEET.
USAF review(s)
completed.
8FlQ1P:
9,
W--tv za if 4 4tJ34-
tND L~zCLd.e:Fica'tt
..,_E-- .-C?: !G i'Ji BY 0a e ,z::P !-NA:. -``H.,.F-- S , ,,:?..l}?i~,~ T,~~~ ~04 1i:~,#1 E.':
10. ON PASS NO. I THE MISSIL1. WAS UN AIRCRAFT POWER. VELOCITY A!
22004/05/1-IA: 3--2---
E
I S C R
Approved For Release 2004/05/13 : CIA-RDP89B00980R000300060103-2 .
Approved For Rel.ee' 200505/13: CIA-RDP89B00980R00Q3W060103-2
1.
S E C R E T
(IN 60767) PAGE TWO
GUIDANCE SLAVING WERE SATISFACTORY. THE MISSILE TRACKED THE
DOPPLER AGGMENTATION.
119 ON PASS NO. 2 AND NO. 3 NO FIRING SIGNAL OR LAUNCH TONE WERE
GENERATED. THE MISSILE REMAINED ON AIRCRAFT POWER. DURING EACH
PASS THE MISSILE BROKE LUCK-ON buT R.EQCQUIRED THE TARGET UPON
RESLAVING. POSTFLIGHT INVESTIGATION REVEALED THAT A SWITCH ON THE
MISSILE TEST PANEL IN THE FCO COCKPIT WAS LEFT IN THE WRONG POSITION
PREVENTING MISSILE TRANSFER TO INTERNAL POWER.
12. A LOW TEMPERATURE WAS INDICATED FOR THE MISSILE GLYCOL COOLANT
THE HEATER CONTROL WAS SWITCHED FROM AUTOMATIC TO MANUAL. JUST
PRIOR TO LANDING AN INDICATION OF INADEQUATE COOLANT FLOW WAS REPORTED.
THE HEATER AND COOLING UNIT WIRE TURNED OFF. A DEFECTIVE COOLANT
.PUMP MOTOR WAS DISCOVERED DURING POSTFLIGHT.
13. MISSILE TELEMETRY, MISSILE BEACON, AND AIRCRAFT BEACON
PERFORMANCE WERE SATISFACTORY. THE FCO REPORTED THAT THE SIGNAL
STRENGTH FROM THE DOPPLER AUGMENTATION APPEARED LOW.
14. INS TERMAINAL ERROR AFTER 1:44 IN THE NAVIGATION MODE WAS
1.6 NAUTICAL MILES.
END OF MESSAGE
Approved For Release 2004/05/13 :CIA-R0P89B00980R000300060103-2