CABLE FROM (Sanitized) TO PRIORITY (Sanitized) INFO (Sanitized)
Document Type:
Collection:
Document Number (FOIA) /ESDN (CREST):
CIA-RDP99B00048R000100110002-4
Release Decision:
RIPPUB
Original Classification:
S
Document Page Count:
3
Document Creation Date:
December 12, 2016
Document Release Date:
January 25, 2002
Sequence Number:
2
Case Number:
Publication Date:
January 20, 1969
Content Type:
CABLE
File:
Attachment | Size |
---|---|
![]() | 159.53 KB |
Body:
Approved For Rehwse 2002/06/24: CIA-RDP99B00048R0Q@10011 00'
2-4
S E C R E T
25X1A
TOR
S E C
NO NITE ACTION
25X1 A , IDEALZ$T
25X1A I. INCIDENT WITH 607
25X1A
JAN 69 CITE
3F!
25X1A
25X1A
sr~~w~w sMr ~
25X1A
DOES NOT APPEAR TO BE F ILLY EXPLAINED
THOUGH THE AIRCRAFT CHECKED OUT SATISFACT-
ORILY ON THE GROUND AND A TEST FLIGHT, I I PE SO NEL
THE INABILITY TO ACCELERATE THE ENGINE IS NOT EXPLAIN-
BY THE
AN 49 RLP
ACTS. YOUR REVIEW OF THE FACTS AND COMMENTS ARE
LICITEU.
2. PILOTS STORY FOLLOWS$ AFTER T/f3 FROM HICKAN, AROUND 55M FT# AT
$29 DEGREES EST FELT A FEW SURGES IN THE AIRCRAFT BUT SAW NOTHING ON
THE INSTRUMENTS. THROTTLE WAS RETARDED TO 50 DEGREES EST. AIRCRAFT
TOOTHED OUT SO THROTTLE LEFT THERE UNTIL RETARDED FURTHER TO MAIN-
TAIN FERRY CRUISE EPR. FUEL CONSUMPTION TRACKED CURVE VERY WELL.
FOR DESCENT THE THROTTLE WAS RETARDED TO IDLE AND BLEED VALVE SWITCH
PLACE IN OPEN POSITION. THROTTLE LEFT IN IDLE UNTIL PITCH OUT IN THE
PATTERN AT ALTITUDE OF ABOUT 11380 FT. AIRSPEED WAS AROUND 93 KTS 50
THROTTLE WAS INCHED FORWARD FOR MORE POWER. RPM WAS 53 PERCENT AT
THIS TIME. NO INCREASE WAS NOTED AND THROTTLE WAS ADVANCED TO FULL
$2 i
SECRET
PAGE I OF 3
Approved For Release 2002/06/24: CIA-RDP99B00048R000100110002-4
Approved For Reese 2002/06/24: CIA-RDP99B00048ROG 100110002-4
25X1A., PA SECRET
OPEN WITH NO ENGINE RESPONSE. THROTTLE WAS RETARDED TO IDLE THEN
"wr AHEAD TO ABOUT 1/4 THROTTLE AND EMERGENCY FUEL CONTROL SELECTED. AS
SOON AS EMERGENCY WAS SELECTED THE ENGINE QUIT IMMEDIATELY. RELIGHT-
ING WAS ATTEMPTED BUT VAS UNSUCCESSSFUL. FLAME OUT LANDING WAS MADE.
THROTTLE WAS NOT RETARDED TO CUTOFF UNTIL AFTER AIRCRAFT HAD STOPPED.
3. MOBIL OFFICER AND OTHER GROUND PERSONNEL DID NOT SEE ANY FUEL
COMING FROM AIRCRAFT IN FLIGHT EITHER ON INITIAL APPROACH DIRECTLY
qw OVERHEAD WHEN ENGINE WAS ONLY RUNNING 53 PERCENT OR AFTER ENGINE HAD
PLATED OUT* WHEN THEY REACHED THE AIRCRAFT ON THE RUNWAY THE BOTTOM
OF THE AIRCRAFT WAS WET WITH FUEL. THE ENGINE COMPARTMENT WAS DREt-'
Ar CHED WITH FUEL AND A SUBSEQUENT' MOTOR ING OF THE ENGINE DISCLOSED THE
SOURCE OF THE LEAK.
A. THE CORRECTIVE ACTION WAS REPLACEMENT OF THE FUEL LINE TO THE P
AND D VALVE? INSPECTION AND SAFETYING OF OTHER CONNECTIONS AND A SUB
SEQUENT ENGINE RON AND TEST FLIGHT.
OHS HERE ARE I
AIRCRAFT
RESPONSE CONCE IVEABLY NOT HAVE FUEL OR VAPORS LEAVING THE
A. COULD A FUEL LEAK OF ENOUGH MAGNITUDE TO PREVENT ANY ENGINE
HAVE ANY SIMILAR CASES OF LACK OF ENGINE RESPONSE AT LOW
32881
SECRET PATE 2 OF 3
Approved For Release 2002/06/24: CIA-RDP99B00048R000100110002-4
Approved For Relwse 2002/06/24: CIA-RDP99B00048ROU0100110002-4
25X1 A FADE
COULD THE F AHE()UT AT ITCHOVER HAVE BEEN CAUSED BY SOME-'
T'HItG OTHER THAN THE FUEL LEAK?
ALTITUDE SEEN EXPERM
S L C E T
END OF MSG
pproved For Release 2002/06/2,6: EIJRIPB91100048R0001c 1W D2!AE OF 3